Реферат: Apollo 13 Essay Research Paper Apollo 13
damaged.
As a result of these occurrences, the CM was powered down and the LM was configured
to supply the necessary power and other consumables.
The CSM was powered down at approximately 58:40 GET. The surge tank and
repressurization package were isolated with approximately 860 psi residual pressure (approx. 6.5
lbs of oxygen total). The primary water glycol system was left with radiators bypassed.
All LM systems performed satisfactorily in providing the necessary power and
environmental control to the spacecraft. The requirement for lithium hydroxide to remove carbon
dioxide from the spacecraft atmosphere was met by a combination of the CM and LM cartridges
since the LM cartridges alone would not satisfy the total requirement. The crew, with direction
from Mission Control, built an adapter for the CM cartridges to accept LM hoses.
The service module was jettisoned at approximately 138 hours
GET, and the crew observed and photographed the bay-4 area where the
cryogenic tank anomaly had occurred. At this time, the crew remarked
that the outer skin covering for bay-4 had been severely damaged, with a
large portion missing. The LM was jettisoned about 1 hour before entry,
which was performed nominally using primary guidance and navigation system.